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Rear End Suspension Link Replacement 3516122 Topic is solved

Help, Advice and DIY Tutorials on Volvo's P80 platform cars -- Volvo's 1990s "bread and butter" cars -- powered by the ubiquitous and durable Volvo inline 5-cylinder engine.

1992 - 1997 850, including 850 R, 850 T-5R, 850 T-5, 850 GLT
1997 - 2000 S70, S70 AWD
1997 - 2000 V70, V70 AWD
1997 - 2000 V70-XC
1997 - 2004 C70

This topic is in the MVS Volvo Repair Database » Delta Link Repair DIY
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Ozark Lee
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Volvo Repair Database Rear End Suspension Link Replacement 3516122

Post by Ozark Lee »

**Editorial Note**

This post was largely a "Stream of Conciseness" writeup and much of the original writeup can and should be ignored. There is, however, other very good information in the thread.


As I’ve mentioned before, I have had a persistent “clunk” in my rear suspension and a “wandering” sensation at highway speeds. I tried the fender washer in the shock mount repair which yielded no change in the sound and then, just to make sure on the easy stuff, I ordered some new shock mounts from FCP Groton. I replaced them and still no change in the clunk.


A couple of weeks ago I decided that a Chief's halftime Sunday project was to find out what the problem was. As soon as I jacked up the car it was apparent, I had over 1 inch (2.5 cm) of vertical travel in my rear trailing arm end links. The right side was the worst as I could actually see the ball joint that should have been immersed in rubber.
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An example of a bad rear endlink.

OEM Volvo links are, at the best price I have found, US $200 each while the aftermarket versions run roughly half of that. Between eEuroparts.com and FCP Groton I ordered the aftermarket versions and new bolts which we shall see if that was a mistake or not. The Haynes manual and Vadis procedures are quite insistent that the bolts be replaced when doing this procedure so I also ordered new bolts for everything associated with the endlink itself.


Disassembly is quite easy. Do the block the wheels, jackstands, etc. Just to get good access I took off the tire and then I first removed the nut (18mm socket) that holds the end link into the “delta arm”. Vadis says to use a “copper mallet or equivalent” to tap out the bolt. I’ve never seen a copper 5 lb. sledge hammer but I used a 5 lb. steel sledge hammer, leaving the nut on, to release the serrated head bolt from the top of the arm. A tip here is to jam a 2 X 4 above the delta link and the bottom of the car. In my case most of the hammer “wham” was diminished by the vertical travel in the suspension if I didn’t jam it.


The next step is to remove the bolt that holds the end link to the chassis, it is also an 18 mm socket. I just used an air impact wrench and zipped it out.
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Endlink to frame bolt removal.

The next step is to remove the bolts from the mounting bracket which are 17 mm socket bolts. In this case I was working on the passenger’s side of the car which is where the fuel filter is bracketed. Take note that you have the fuel filter and the fuel lines in close proximity to the link, it will be important later on. I also removed the fuel filter bracket which requires a 12mm socket. I also used a T-27 Torx driver to remove the parking brake cable from the bracket.
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End link bracket bolts.


I then removed the bolt securing the fuel filter using a 12mm socket and let the bracket drop and hang.
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The end link with the bracket removed.


The next step is to pry downward on the end link so as to release it from the chassis for removal. Use a pry bar, a crow bar or a pipe, it should pop right out.


At this point Vadis calls for me to utilize Volvo tool # 999 5497 to remove the endlink itself. I looked in every drawer of my toolbox, twice, and I don’t have Volvo tool # 999 5497. I decided to improvise.


Note: (3.5 hours of trial and error and swearing followed this step)


After chiseling, prying , cussing, etc. the endlink refused to come out so I enlisted the trusty come along. I looped a steel cable around the top and the bottom of the link and then hooked it to the come along that was hooked to the frame of the ¾ ton Suburban that was parked next to the Volvo. It makes good ballast.
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Steel cable around the endlink, a ¼” cable secured through the bushing would likely work as well.
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The come along tied between the Suburban and the Volvo.

At this point I started to ratchet the come along and found that the delta arms were moving much more than I was comfortable with so I ran a chain through the delta arm and tied the chain through the tow hoop at the back of the trunk (boot?) so as to limit the forward travel of the arm.
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Chain through the delta link.
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Chain through the tow hook at the rear tow hoop of the car.


I just tied the chain in a knot to secure it through the hoop. Following Lee’s law on knots, if you can’t tie a good knot, tie a lot of them.


I next proceeded to increase the pressure with the come along which nearly took the car off of the jackstand. I added a safety jackstand and tried again to extract the endlink only to get nowhere.


A propane torch is your friend.


In looking at the (albeit ScanTech) replacement endlink I noticed that it was a rubber center with a plastic outer shell. I also noticed that the actual delta arm was aluminum so banging on the delta arm was likely only going to dent it and make the extraction harder. I fired up the torch (remember that you earlier took note that the fuel lines and fuel filter were hanging next to the link) and proceeded to heat the crud out of the delta arm. I still had it under considerable tension with the come along. To my delight plastic began to ooze from the end of the link which meant it was a thermoplastic and it would melt. Once I got it hot enough, and it oozed enough, I took a cold chisel and gave the whole mess a big whack and, just like magic, the end link freed itself from the delta arm.


Note: My attorney has advised me that the preceding procedure should never be done and that it is imperative that you purchase Volvo part number 999 5497 when attempting to remove an endlink.
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The old endlink.
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The new endlink.


Now, for the next trick, reinstall the new endlink. I tried for quite a while to feed the new endlink into the delta arm. I cleaned up the melted plastic residue out of the inside of the arm and tried (an hour or so) various methods of lining up the link and then whacking it in with a hammer. Frustrated, (cussing), I looked at the OEM endlink and found that they had beveled the leading edge of the plastic at the Volvo factory. Next stop was the grinder to bevel the leading edge of the plastic on the ScanTech replacement. If you don’t have a grinder you can bevel it with a file or even a pocketknife.


Even with the beveled edge I had a terrible time trying to get the link aligned to tap (smash) in with a hammer. The outside edges would catch but I noticed that I had clearance at the top and the bottom so I enlisted a 2 ¾” hose clamp. I set the hose clamp at roughly ¼ inch (6.5 mm) in from the inside end of the endlink plastic. By adding pressure to the hose clamp I was able to get the shape of the plastic housing to a point where it drove in, quite easily, to about the halfway point.
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The hose clamp “former”.


I didn’t gain much ground over the halfway point of getting it installed. I was using a hammer on the end of the endlink which is encased in rubber. The rubber was absorbing the force of the hammer and not transferring it to the outside shell. I then enlisted a small (1/2”) pipe to tap the outside edges of the plastic shell frame rather than the outside steel link itself. It is a walk on procedure where three taps on one side followed by three taps on the opposite side (rinse, lather, repeat) ultimately gets it on all the way.


From here it is a matter of bolting everything down. I started by prying the link end itself back onto the stud and then loose fitting the mounting bracket back to the chassis. Using my new bolt I then torqued the end link to chassis bolt to 105 Nm and then added 90° of angle torque. Next I tightened the mounting bracket to 65 Nm + 60° of angle torque and lastly I tightened the end link to delta link bolt to 65 Nm +120° of angle torque.



Carefully remove the chain so as to not damage the brake line and re-attach the fuel filter mounting bracket. This is what is should it should look like after repair.
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A fully repaired endlink. Notice the difference between this link and the original.


This is a BI itch of a job that took every tool in my toolbox and then some. I only got one link done today working from 11 AM to 7 PM. With what I’ve learned I estimate that the next one will take about 3.5 to 4 hours. Next stop, after I repair the other link, is the alignment shop to get the rear end aligned.



...Lee
'94 850 N/A 5 speed
'96 Platinum Edition Turbo
Previous:
1999 V70XC - Nautic Blue - Totaled while parked.
1999 V70XC - RIP - Wrecked Parts Car.
1998 S70 T5
1996 850 N/A
1989 740 GLT
1986 740 GLT
1972 142 Grand Luxe

MadeInJapan
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Post by MadeInJapan »

Wow...very nice write-up. Don't know if I would ever try this myself though...I'm gutless. Anyway, someone probably can use this information so I'm pinning it in the Repair Database.
'98 S70 T5 Emrld Grn Met/Beige Tons of Upgrades Mobil-1
'04 V70 2.5T Red/Taupe Some Upgrades Mobil-1
'07 S40 T5 AWD 6 speed manual! Silver/Black Stage1 Heico & Elevate
'07 S60 2.5T Blue/Taupe- my kid's Volvo

CarVolvo
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Post by CarVolvo »

Good timing.. i just removed the complete trailer arms from my 95 parts car.

Not sure if you tried this but i removed the big bolt on the end link and the supports. I put my foot on the trailer arm and rocked it up and down.. and after the 3rd rock..... ***splunk*** it came right off.. the ridges where the trailing arm is hooked on to seems to catch it.

I am really surprised how the whole system was held on with the shock absorbers and this trailing arm link... makes the ride smooth but really makes you aware how you need to keep you shock absorbers in good shape.

The rear springs were also easily replaced with this type of system... every time i work on these cars i am amazed at their engineering!

Good work Lee!
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Ozark Lee
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Post by Ozark Lee »

I hate to bump the thread but I did the (US) drivers side today and it took about what I thought, 3.5 hours. A couple of things I can add is that instead of worrying about the fuel line on the right side of the car you need to worry about the brake line on the left side. I folded a piece of galvanized roof flashing to serve as a heat shield and just wedged it in between the brake line and the delta link while torching it.

I also found a real nifty way to press out the bolt that holds the end link in place. Yesterday I helped my son change out the U-Joints in his Jeep and I rented a U-Joint press from O'Reilly Auto Parts. It is like a giant "C" clamp with a loop at the base and it works perfectly to press the bolt out rather than to beat it out with a hammer. I think they charged my credit card US $265.00 but they credit it back in full when you return the tool.

...Lee
'94 850 N/A 5 speed
'96 Platinum Edition Turbo
Previous:
1999 V70XC - Nautic Blue - Totaled while parked.
1999 V70XC - RIP - Wrecked Parts Car.
1998 S70 T5
1996 850 N/A
1989 740 GLT
1986 740 GLT
1972 142 Grand Luxe

mazda4d
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Post by mazda4d »

I think I found the Volvo tool # 999 5497 in the trunk of my car :D

Part is removed for clarity (i.e. I took the picture after it worked)
This was done two month ago.

Image

As you can see on the picture everything is there except the bushing, but it used to have the black steel rod through the main hole (it was between the jack and the red square steel feet, where the handbrake cable now is).

So I used the car jack as a puller by jamming it between an angle iron (1"x1"x12") and a 1/2" steel rod the went through the bushing. I used a piece square tubing (red) to counteract the jack force so that it would pull straight. The angle iron goes through the triangular hole in the delta link.

The best way to do this would probably be to use two standard scissor jacks (one on each side) rather than trying to push against a bar at

logie
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Post by logie »

hi there new to site just renewed end link bushes not too bad a job as the old bushes were scrap i just dug out the rubber bush with old screwdriver .only problem was the side with the brake pipes dont want to bend them too such
spent about 3 hr each side. New bushes do not come new bolts bought from europarts .went in by local volvo stealer to get new bolts as manul recomends
new bolts, dealer would have to order but they said that they do not replace bolts when changing bushes. anyone thinking of doing job just take your time
make sure car is well supported on stands and you will be ok

chax
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Post by chax »

Thanks, Ozark Lee!
SOME NOTES:
- Careful with the torch: the undercoating on the trailing arm can start burning, so wirebrush off as much as possible first, and keep a fire extinguisher handy. I used a torch for about 2 minutes, but didn’t get any results.
- I used a drill to dig out the thermoplastic part of the link: forcing the bit against the top and bottom of the cavity allows you to spray in some silicone, which I assume helps loosen the link. When I do the other side, I might try hammering a scraper in between the thermoplastic and the trailing arm…just to see if it helps.
- For pulling pressure, I used my V70: after securing the trailing arm to the trailer mount on my 850, I ran a nylon strap through the towing loop on the V70, wrapped it around the link, moved the V70 enough to put a decent amount of pressure on the link, then went back to work on the thermoplastic with the drill: drill a bit, sledgehammer the link left, then right, repeat. This eventually worked.
- I did the right side today; what I might try before doing the left side is to remove the bolt that attaches the link through the trailing arm, replace it with a bolt with about half the diameter, then drive the car around a bit: hopefully, the play the smaller bolt will provide (don’t want the arm to outright fall off!) will be enough to loosen the link.
- When installing the new link, I recommend using Ozark Lee’s method wherein he “walked” the new link into its cavity using a pipe on the thermoplastic on one side, then on the other. I sledge-hammered mine directly on the end of the link, and although the hole in the link lined up with the hole in the trailing arm, the thermoplastic isn’t completely seated in the cavity, making me wonder if it’s possible that the sledgehammering could have damaged it. If it still isn’t seated tomorrow (driving it around today might have already seated it), I’ll probably use this method to try to walk it in the rest of the way (~1/4 inch).
- Final note: I had decided to replace the links because the car has been taking bumps way too hard ever since I got it (4/08), even after I changed the front struts, cushions, and mounts, and then the rears with touring grade shocks. Being fed up with the harshness of the ride, and assuming it must be the links (they’re 16 years old!), I bought a pair. But when I removed the right link today, it seemed to still be pretty sturdy. The ride after replacing this link seemed a bit tighter, but still just about as harsh as before. I’ll update, once I replace the left side link.

plankton
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Post by plankton »

MadeInJapan wrote:Wow...very nice write-up. Don't know if I would ever try this myself though...I'm gutless. Anyway, someone probably can use this information so I'm pinning it in the Repair Database.
that is precisely the problem I have with my 99 v70...perfect tutorial sir!

Lets "get 'er done" !
Thanks for sharing.

JimBee
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Post by JimBee »

Perusing this fix, I'm thinking that a piece of square tubing, drilled through to accept a bolt through the link and slipped over the link end with the bolt through it; then a piece of angle stock bolted to the underside of the square tubing for a bfh treatment, might help.

jakub72
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Post by jakub72 »

Just coming off the rear end suspension fix high from Sunday. Started at 2 finshed by 11.......

The best way to deal with the delta links is heat. After installing them very carefully and slowly with gentle taps from both top and bottom, to walk them in; I realized why nothing else worked. It is a very tight fit and I bet pulling them out would require the same amount of alignment. I did try the puller method by welding a bracket around the arm and nut welded to a rod, but all it did was bend a #10 threaded rod and break welds. I finally got pis#ed and cut it off. I then drilled a bunch of holes in the plastic and turned on the heat. The plastic evetually does melt and I then picked the plastic out with screwdrivers and needlenose pliers. The other side I drilled one hole and more heat.....presto!!! When assembling I used lots of love and plenty of lube......tire shine worked good. I could do the next one in 3-4 hours for the entire suspension.

Over all worth the work and hassle...no clunking, no drifting and finally the car does not pull to the left under hard braking from the rear.

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